The Pluto LNG turnaround was completed as planned but the mixed refrigerant compressor has experienced vibration on restart. As a result, further activities extending the turnaround have commenced to achieve the restart of production, targeted for the end of June 2019.
Woodside has made arrangements to meet obligations to its customers, including the purchase of third-party cargoes.
Due to the turnaround extension, Woodside’s 2019 production is expected to be at the lower end of the 88 – 94 million boe guidance range.
Read the article online at: https://www.lngindustry.com/liquid-natural-gas/11062019/pluto-lng-turnaround-extended/
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